Development and Testing of the Upgraded High Pressure Turbine Section for an Industrial Gas Turbine

2008 
As part of an ongoing development program to increase power output and efficiency of the THM 1304 gas turbine, modifications were made to the high pressure turbine. The modifications include but are not limited to blade and vane aerodynamics, cooling system and clearance control, mechanical design and materials. The development was to achieve the following goals: • Intensified blade and vane cooling to permit higher turbine inlet temperatures and to further extend service lifetime; • Improved aerodynamic performance; • Blades with pre-loaded tip shrouds to achieve low vibration amplitudes in a broad operating speed range; • Rotor design modifications to simplify assembly and disassembly; • Modified vane carrier and casing designs for optimal tip clearance control and turbine performance. The improved high pressure turbine was extensively tested in MAN TURBO’s full-load gas turbine test facility. Test results verified that component temperatures were within the expected range and design targets have been achieved. The first production gas turbine equipped with the upgraded high pressure turbine was installed in May 2004 as a gas compressor driver. To date a total of 11 units have gone into operation including units for power generation. Dry low emission technology is used on all engines. Every unit is monitored by an online data monitoring system and visually inspected in shorter intervals to verify the behavior in the field. Operation of the fleet is flawless at this time.Copyright © 2008 by ASME
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